Just got it a day ago... Took some crashes but everything was fine till the camera screw went inside the drone its self... I managed to get it out but now when I try to fly it the back of the quad copter over powers the front... I've tried resetting it but it does not help.... Please help?
Sounds like the IMU was somehow compromised - if so, the only thing that will fix is a new main board. Since it's broken you might as well try some crazy stuff like knocking it against a table (the G-Force may reset the IMU)...also reset it a number of times. Check the trim carefully - maybe you can fix in the trim? Also, try resetting with something that lifts the front up a bit (as opposed to perfectly level).